• 0-35V 0-5A Lab PSU CS FL-305

    From G8MNY@21:5/101 to TECH on Sat Jun 29 05:32:55 2019
    R:190629/0822Z @:LU4ECL.LP.BA.AR.SOAM #:19567 [19568] FBB7.01.35 alpha $:10394_ R:190629/0813Z 31865@N3HYM.MD.USA.NOAM BPQ6.0.18
    R:190629/0822Z @:CX2SA.SAL.URY.SOAM #:8939 [Salto] FBB7.00e $:10394_GB7CIP R:190629/0818Z @:GB7CIP.#32.GBR.EURO #:10394 [Caterham Surrey GBR]

    From: G8MNY@GB7CIP.#32.GBR.EURO
    To : TECH@WW

    By G8MNY (Updated Oct 17)
    (8 Bit ASCII graphics use code page 437 or 850, Terminal Font)
    Here is a very unusual circuit principles, of this Italian 0-35V 0-5A PSU. It uses a transformer variac secondary to make an efficient linear regulator PSU, together with variable current limiting & dissipation power fold back.

    ┌────────────────────────────────────────────┐
    │┌───────┐ ┌───────┐ ( ) FL-305 │
    ││ \ V │°│ \ A │ Fine V ___ │ It was all blown up &
    ││ \ │ │ \ │ .- -. │ modified into a simple │├───────┤ ├───────┤ / Course\ │ raw PSU. So I did a lot │└───────┘°└───────┘ \ V / │ of reverse engineering,
    │ overload ( ) '-___-' │ to find out it how it
    │ on trip sw A │ originally worked, before
    │ ! ┌────┐ + - e + - │ attempting the restoration.
    │ ° ° └────┘on° (o)(o)(o)(o)(o) │ └────────────────────────────────────────────┘

    SCHEME 15A Power NPN 15A L──o-o─┐ 6-42V AC Darlington__ Amp Trip
    2A )||(<───────┐ ┌──┬──────┤~~~\_/e ├─Rshunt─Meter─┬────┬────┬──\── +ve Mains _)||( \ ~│15A│+ │8-60V │ │ │ │ Control │
    )||( Var Bridge │ │ Drive ├────Imon──────┤ PSU 0V! │ 0-35V
    ON )||( R ~│ │- │ │ │Out │ Volt
    N___ \_)||(________│ │ ===16mF │+In Out│ Vmon Meter 0-5A

    || ___ │ │ 65V └Drop Mon┘ │ │
    300W ||(30V Control └──┴──────────────────────────────┴─────────┴──\── -ve E─┬──e └─── +/-12V PSU
    ///

    The coarse Voltage Variac control has stops on it to give between 6V - 42V AC, & a 50K Var R to control the course regulated Volts. Unusually a separate 30V winding is used to make a floating +/-12V @ 40mA zener PSU on the +ve O/P rail, for 5 Op amps, 6 transistors & 3 LEDs of the complex control circuit.

    The 1st Op amp with input protection diodes & 1K Rs, monitors the output Volts, compares PSU -ve through VarR & Fine VarR to +ve from 5K preset & 5K6 using +6V zener reference. And with 2 transistors it shunts away the 3mA drive to the darlington, & lights up the green OK LED.

    +12V───┬───2k7──┬─470─>Darlington Base 0-3mA
    Voltage Comparitor ┌────────)────────┤ (Or a Mosfet)
    │\ │ │ │ /│
    +6V 0V─1K─┬──┬─┤+\ │/e 1K2 e\│ /+├
    │ preset /_\\~/│1 >─┤<├─┤PNP ┌──┴──┐ PNP├─┬─┤>├─< 2│ Current Limit
    └5k6──5K──┬─1K─┴──┴─┤-/ │\ OK OVERLOAD /│ │ \-├ Comparitor
    2K │/ │ LED LED │ │ \│
    Fine VarR 10K │ │ 10K │
    │ │ │/ \│ │ │ /│
    50K ├───┤NPN NPN├───┤ │ /+├
    Course VarR │ │\e e/│ │ └─┤>├─< 5│ Power Foldback
    │ 10K │ │ 10K \-├ Comparitor
    -Ve -12V──┴─────┴─────┴─────┘ \│

    A 2nd Op amp monitors the output current & compares it to the current set pot & -6V ref zener. Overloads, limit the drive current & with 2 more transistors, by again shunting away the 3mA darlington drive, & lighting the red OVERLOAD LED, instead of the green OK LED.

    A 3rd Op amp monitors the voltage drop across the darlington pass transistor. And converts this into current to feed the emmitters of a "dual transistor long tailed pair" mixer, with a sample of PSU O/P current into one of the bases.

    Darlington ┌───┬───+12V Power Dissapated │\
    Volts Monitor 10K 10K │\ 0V─1K─┤+\
    ┌───68K──┐ ├───)────────────────┬───┤+\ │5 >─ Power
    ││\ │ │ │ │ │4 >─┬─680──┬──┤-/ Foldback +Out─680K┴┤+\ │ │ ├────────────────)─┬─┤-/ │ 3K3 │/ Comparitor
    │3 >┬6K8┤ │/ V&I \│ ┌─1K5─+Out │ │ │/ │ │
    +In──680K┬┤-/ │ │ ┌─┤ Mixer ├─>Ipot │ └───10K┘ 5K
    ││/ │ │ │ │\e e/│ 100 10K preset Set Max Power
    └─68K┘ └─)───┴───┘ │ │ │ Dissapated
    └─────────────┴──────────┴<+ve & 0V -6V

    The resulant balanced mix product, feeds the 4th Op amp, to give an accurate signal proportional to the power being dissapated. And that then feeds the 5th Op amp & also uses the -6V to set the Max Power Dissapated, & also light the OVERLOAD LED.

    CALIBRATION
    A high power DC load is needed, I used a large tapped WW resistor 2+2+4Ω 1kW. Set the start position of the Variac VarR, & then the 4 presets are used to determine, 1 Max overhead voltage, 2 Max Current range, 3 Current foldback sample Ipot, & 4 Max foldback power. When correctly set the head voltage is always just enough for a cool regulator at all output voltages & currents!

    DOUBLE CURRENT MODIFICATION
    As the PSU has a hugh mains transformer & a roomy chassis, I decided to see if it could be made to do 10A! (350W Regulated DC O/P!)

    1/ Transfure the 2 heatsink reverse voltage protection tab diodes to the PCB,
    as they don't need heatsinking.

    ┌┴┴┴┴┴┴┴┴┴┴┴┴┴┴┬─────┬───┬───┬┐
    ││ pcb ││ C │pot├─Br┤│ 2/ Re-use the 2 spare heatsink holes for 2 │~~~~~~~~~~~~~~└┬───┬┘~T~ │ more NPN insulated Darlington 15A
    │ _ _ _ _ Rs ┌─────┴─────┐│ transistors, pointing away from each other, │(_)(_)(_)(_) ▌ │ VARIAC ││ to spread the heat.
    │ Cs ▌ │TRANSFORMER││ File rear case hole to give clearence, &
    │ ┌┴─┴┐ ┌┴─┴┐▌ │___________││ wire them up in parrallel to PCB, with a 3A └┬┴───┴┬─┬┴───┴┬┬┬───┬─┴─┬────┘ fuse in each emmitter, as current share Rs.
    ~~~~~ ~~~~~ └┘ └───┘
    3/ Remount 16mF C & bridge, from PCB metal panel, on to the rear case either
    side of the VarR, making sure the piller mounted PCB will fit back OK.
    4/ Remove the PCB metal panel, & add more main 65V smoothing (I used 4x 5mF) in
    the new space, to maintain low DC ripple @ 10A before regulation.
    5/ Shunt 5A meter with resistance wire to now read 10A FSD, & re-label 2x/10A. 6/ Shunt the large current sampling 0.1R with resistance wire to bring it down
    to < 0.06R, & mount it with the left over pillers behind Amp meter mounting
    screw.

    Then do the calibrations again with current limit set to @ 10A max, & the fold back current to 1.5A when set @ 35V. It is all just doo able, right on the limit of the PSU & still not running too hot.

    CONCLUSION
    This is now quite usefull bench test PSU, able to test low current circuits with the new current limit from "10mA to 10A" @ voltages from "75mV to 35V". Used for testing prototypes, zapping & charging batteries, run modest power rigs (30W) etc.

    Be aware not to over voltage kit, as it is a Lab PSU not just a Rig one!

    If it is often to be used at this "higher power limit", a 60°C thermal trip glued on the transformer might be a good safety feature to add!


    See also tech buls "Lab PSU", "Simple 20A PS", "High AMP Crowbar Protected PSU"

    Why Don't U send an interesting bul?

    73 De John, G8MNY @ GB7CIP


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